Todays update: Parts and shakedown weekend
Ok, cant be too long but an update has been over due..
Friday evening I got home from work to find a missed parcel note from FedEx saying bits from america had arrived..
I had to load the car, sort my hydro issue, swap my front wheels, drive an hour to matt carters to help Dylan and autodanny remove the cage from yoshi.. and all before 8pm.. It was 6.45 when I got the note form fedex.
..naturally, I decided screw all that and drove to the fedex office to collect my goodies! lol
Priorities an all.
Got there.. got my package and found these SEXY things inside..
M.A.S.S.I.V.E thank you to Justin Pawlak for putting these together for me, sorting out all the sourcing crap and then spraying them without me even asking!!
Cant wait for the next delivery.
Hoping to get these on before the end of the week (Hi Dylan!!
)
Went over to matts stupidly late after sorting all my stuff for the weekend and found Dylan,Matt and Danny had litteraly just finished up removing the cage, so i brought maccy D relief lol.
Saturday morning we went and picked up another S body for the TG massive as Daz had bought a project 13.
then some fettling on the cars like re-bleeding brakes and other bits and loading up matts s14 then off to pod.
Shake-down 1: POD
Pod was er.. interesting. It was foookin packed, it was rubbishy weather being bright then rain then bright then hail then cloudy n all that crap.
Add to the traffic at pod some teething issues with the car.. Pod was the first time I had tried 17s on the boggo FC powers.. and it struggled. Or I thought it did.. after some scary loss-of-power moments and bogging down/resistance we had brainstorming and narrowed it down to fueling. I had not drifted on less then a 3rd tank before and with no time to go fill up and try.. I just 'hoped' that was it and would find out tomorrow.
The only other issue was scrubbing.. It seemed my arch mods were not high enough OR the coils needed more dampening/preload. Apart from that she seemed ok.. snappy at times but that seemed to be down to the power delivery/fuel issue.
so a Mixed testing session.
Headed off from Pod to Jords house as a 'over-nighter' before norfolk. On route however my frikkin sideskirt decided to do a 'fuck you' moment and flew off behind me on the motorway...
..where it promptly got owned by an artic lorry. In fairness it could have been alot worse, it only caught one side, so I threw what I had recoved in the car and headed onto Jords.
Jords
After I arrived I asked if he had a hammer i could mod the arches with and a few cable ties to rebuild the skirt (as I had run out during day) and he offered for us to take it to his workshop!
Sure enough we did where moocho fettling occured.. the photos of which you have probably seen earlier in the thread. Arch problem not solved but severly reduced to nearly perfect, the front wing was catching on passenger door so we sorted that, few other minor tweaks and then finally rebuilt the skirt.
big thanks to him for the help, the spare bed for the night and to his good lady Naomi for the dinner..
oh and the dog for the leg loving..
Norfolk
Well.. what can I say. Massive change from the saturday. Loverly weather.. frikin TONS of track time! Big thx to Roger Cooling and his crew for the help, the tyre lending and general friendlyness.
Car did very well, especially in the heat. only issue to arise was a seeping oil leak from turbo feed which I sorted. Seems to do well on the 17s even with the massive 235/45's on an 8j. lol tractor spec yo!
hoping the 225s on the 9j/10j shouldnt scrub and be good for round one. Only time will tell.
Further update after tonights fettling