So, where do I begin! The day started off a little rushed. The car has always squealed on start up which I have always put down to a slightly slack power steering belt as there isn’t any more room of the tensioner. Prior to Rockingham I did buy a smaller belt, so thought I’d swap this over before starting the day to avoid any drama’s.
Once the track opened, I opted to take the car down the road and back to get a quick feel of the chassis, do some steady figure of 8’s to bed the diff in some more and get everything up to temperature. The car felt ok, and it was time to que up.
In the que I started to learn the cars traits, noises and vibrations as everything was so different to my old chassis. I told myself that the first lap would be a sighting lap, get used to the boost levels and feel the chassis. So as I was told to go, the right foot when down and the boost came on. Turned into the corner as expected, and I just dropped the clutch. I don’t know whether it was the excitement to feel the car or the itch to be sideways again. Either way, it was so fun! It wasn’t the cleanest lap I didn’t really know the layout apart from the visuals given in the briefing. But it felt good!, and I felt comfortable straight away.
Throughout the day I began to experiment with my lines, being more aggressive on entry (zero use of the handbrake) and practicing tandem runs with friends. The latter of which I really didn’t think I would be doing on the first outing but I welcomed it. The car ran faultlessly all day bar one bolt rattling loose. The chassis felt incredible. It’s really positive and responsive, you can feel a lot which I love. The motor which night and day over my old SR20 setup which you’d expect and he noises it makes are to die for. Now, my only criticism is the motor didn’t scare like I thought it would have done. Maybe I was expecting too much, or maybe it really is underperforming. Anyway, the day was great and it was time to pack up unfortunately.
So once I got back, it was the usual drill. Off load the car and put the tools away but I couldn’t help think about the motor and whether it was underperforming. If so, why? This seems to be the biggest question that nobody can definitely answer.
Whilst I was racking my brains every day, I thought it’d be a good idea to send the turbo off to get some minor upgrades. So, we started off with a standard TD06SL2-20G:
I was amazed how fast the whole setup comes off. I think it was sub 10 minutes and the turbo was off?!
After speaking to Liam @ Midland Turbo, we decided to change both the compressor and turbine wheel to help give the TD06 a bit of extra punch all round, as well as a full rebuild with better internals.
Below show the differences between the turbine wheel. The original TD06SL2-20G uses an 11-blade wheel to help with the spool on a 2.0L engine. We opted to change to a 9-blade turbine wheel. Reason being, less blades equals more flow. Liam said he had done this swap on another customer’s TD06 and found it gave the 20G a much larger punch, this sounds fun!
Old Turbine Wheel vs New Turbine Wheel
Next up was the compressor wheel, where we opted to use a Billet item. Now the performance gain should come from the fact the lower tips are extended past the compressor housing, and the overall depth is quite a bit bigger. This in theory should equal to more flow, which means more power!
And just some picture’s Liam sent me once the unit had been rebuilt:
After a little bit of fiddling around, the TD06 was back on and ready to fire up again. All I can say is top mounted turbo’s make life so much easier when it comes to the mechanical side of things!